Iron Production Experiment Nov 2005
Date: 12 Nov, 2005
Location: Vinderheima
Premise:
We decided on two variables only, one major one minor :
1) Reuse a smelter structure. This entailed repairing the inner wall of
the smelter around the tuyere. A depth of about 1 1/2" of
new clay was applied to replace the material eroded from the
earlier smelt. We had high confidence that this would not create a
major problem, as archaeology shows this process, even several times
over. The clay body used was the same as used to create the initial cob
structure.
2) Use of one of the pottery kiln shelf support tubes as the tuyere.
These were 2" OD and that magic 1" ID. The material was rated to 1250 C
- which puts it into our operation range for the smelter. Again our
confidence was high that this would perform well.
We had re-lined the smelter about a week before the smelt with pretty
wet clay, and patched some cracks from the outside. Afterwords wrapped
the structure up in its protective plastic bag. The repair area was
still soft enough to take finger dints when we started.
In addition to these variables we decided to confirm our air
flow numbers so that we can work on getting the bellows producing the
correct flow.
Experiment Notes - Norse Short Shaft Smelter
The Team:
Leader |
Darrell Markewitz |
Staff |
Kevin Jarbeau Dave Cox Ken Cook Steve |
Recorder |
Neil & Karen Peterson |
|
Reports of all of our iron smelting efforts along with more articles and information are available on the "Iron Smelting in the Viking Age" CD from the Wareham Forge. Copies of the CD can be purchased here. |
Setting up the smelter:
This was easy this time. Patching the inside and outside of
the wall near the tuyure. A few other small patches were put
in place.
A forty-five minute pre-warm was done
with wood splits. Since we were waiting - what's a fire without some jiffy-pop! We've got to get around to asking them to help sponsor us...
It should be noted that due to a minor miscalculation we ran out of
prepared taconite ore. As a result we switched over to
virginia rock ore part way through (the ore charges are identified
below). In addition some gromp was added towards the end of
the burn.
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Patches around tuyere |
Adding charcoal |
First tapping |
Auto-tapping |
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Cooled autotap |
Burning well |
Burn down |
Pulling the bloom |
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Consolodating |
Measurements |
The morning after
As usual we deconstructed the site the morning after the smelt taking a
variety of measurements to assist in our experiments.
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Light slag |
Wall top |
Above tuyere |
Tuyere comparison |
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| |
Double wall |
Double wall |
Time |
Event |
Air Flow |
Measures |
Relative |
Absolute |
Total |
Relative |
Elapsed |
Charcoal |
Ore |
0:00 |
00 |
addition rough charcoal,
occasional gentle air blast (begins at 1135h) |
B |
|
|
|
|
0:25 |
00 |
Increase air flow |
C |
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|
|
0:38 |
32 |
first graded charcoal added |
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|
|
|
0:44 |
19 |
Increase air flow |
C+ |
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|
0:48 |
10 |
charcoal |
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1 |
5 lbs* |
5 lbs |
|
0:58 |
10 |
charcoal |
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2 |
5 lbs |
10 lbs |
|
1:04 |
|
seed charge |
|
1 |
.75 lbs* |
|
.75lbs |
1:06 |
8 |
charcoal |
|
3 |
5 lbs |
15 lbs |
|
1:14 |
|
seed charge |
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2 |
.75 lbs |
|
1.5 lbs |
1:15 |
9 |
charcoal |
|
4 |
5 lbs |
20 lbs |
|
1:21 |
|
seed charge |
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3 |
.75 lbs |
|
2.25 lbs |
1:25 |
10 |
charcoal |
|
5 |
5 lbs |
25 lbs |
|
1:31 |
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seed charge |
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4 |
.75 lbs |
|
3 lbs |
1:33 |
8 |
charcoal |
|
6 |
5 lbs |
30 lbs |
|
1:37 |
|
seed charge |
|
5 |
.75 lbs |
|
3.75 lbs |
1:41 |
8 |
charcoal |
|
7 |
5 lbs |
35 lbs |
|
1:50 |
9 |
charcoal |
|
8 |
5 lbs |
40 lbs |
|
ore charge (+ one and a half scoops added in this time) |
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6 |
1.1 lbs+ |
|
4.85 lbs |
1:58 |
8 |
charcoal |
|
9 |
5 lbs |
45 lbs |
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ore charge (++ two scoops plus the left overs from above) |
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7 |
1.9 lbs++ |
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6.75 lbs |
2:06 |
8 |
charcoal |
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10 |
5 lbs |
50 lbs |
|
ore charge |
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8 |
1.5 lbs |
|
8.25 lbs |
2:13 |
7 |
charcoal |
|
11 |
5 lbs |
55 lbs |
|
ore charge |
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9 |
1.5 lbs |
|
9.75 lbs
|
2:22 |
9 |
charcoal |
|
12 |
5 lbs |
60 lbs |
|
ore charge |
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10 |
1.5 lbs |
|
11.25 lbs |
2:30 |
8 |
charcoal |
|
13 |
5 lbs |
65 lbs |
|
ore charge |
|
11 |
1.5 lbs |
|
12.75 lbs |
2:38 |
8 |
charcoal |
|
14 |
5 lbs |
70 lbs |
|
ore charge |
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12 |
2.25 lbs |
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15 lbs |
2:45 |
7 |
charcoal |
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15 |
5 lbs |
75 lbs |
|
ore charge |
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13 |
1.5 lbs |
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16.5 lbs |
2:53 |
8 |
charcoal |
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16 |
5 lbs |
80 lbs |
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ore charge |
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14 |
2.25 lbs |
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18.75 lbs |
3:02 |
9 |
charcoal |
|
17 |
5 lbs |
85 lbs |
|
ore charge |
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15 |
2.25 lbs |
|
21 lbs |
3:10 |
8 |
charcoal |
|
18 |
5 lbs |
90 lbs |
|
ore charge |
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16 |
2.25 lbs |
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23.25 lbs |
3:18 |
8 |
charcoal |
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19 |
5 lbs |
95 lbs |
|
ore charge (1 scoop taconite, 2 scoops virginia rock ore) |
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17 |
2.25 lbs |
|
25.5 lbs |
3:26 |
8 |
charcoal |
|
20 |
5 lbs |
100 lbs |
|
ore charge (virginia rock ore) |
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18 |
2.25 lbs |
|
27.75 lbs |
3:36 |
10 |
charcoal |
|
21 |
5 lbs |
105 lbs |
|
ore charge (virginia rock ore) |
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19 |
2.25 lbs |
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30 lbs |
3:38 |
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Scoop of gromp added |
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3:41 |
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Rogering the tuyure |
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3:43 |
7 |
charcoal |
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22 |
5 lbs |
110 lbs |
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ore charge (virginia rock ore) |
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20 |
0.75 lbs |
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30.75 lbs |
3:50 |
7 |
charcoal |
|
23 |
5 lbs |
115 lbs |
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ore charge (virginia rock ore) |
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21 |
1.5 lbs |
|
32.25 lbs |
3:58 |
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charcoal |
|
24 |
5 lbs |
120 lbs |
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ore charge (virginia rock ore) |
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22 |
2.25 lbs |
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34.5 lbs |
4:06 |
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charcoal |
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25 |
5 lbs |
125 lbs |
|
ore charge (virginia rock ore) |
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23 |
2.25 lbs |
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36.75 lbs |
4:16 |
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charcoal |
|
26 |
5 lbs |
130 lbs |
|
ore charge (virginia rock ore) |
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24 |
2.25 lbs |
|
39 lbs |
4:24 |
|
charcoal |
|
27 |
5 lbs |
135 lbs |
|
ore charge (virginia rock ore) |
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25 |
1.5 lbs |
|
40.5 lbs |
4:25 |
|
ore charge (virginia rock ore) |
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26 |
0.75 lbs |
|
41.25 lbs |
4:28 |
|
ore charge (virginia rock ore) |
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27 |
0.75 lbs |
|
42 lbs |
4:36 |
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Begin adding gromp pieces |
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4:37 |
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charcoal |
|
28 |
5 lbs |
140 lbs |
|
4:42 |
|
charcoal |
|
29 |
5 lbs |
145 lbs |
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4:45 |
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Add remaining gromp (total 1.1 kg) |
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4:47 |
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reduction charge |
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28 |
1.5 lbs |
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43.5 lbs |
4:48 |
|
charcoal |
|
30 |
5 lbs |
150 lbs |
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4:57 |
|
charcoal |
|
31 |
5 lbs |
155 lbs |
|
5:07 |
|
charcoal |
|
32 |
5 lbs |
160 lbs |
|
5:16 |
|
charcoal |
|
33 |
5 lbs |
165 lbs |
|
5:25 |
|
charcoal |
|
34 |
5 lbs |
170 lbs |
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5:35 |
|
charcoal |
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35 |
5 lbs |
175 lbs |
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air flow reduced to minimal - remaining charcoal removed |
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consolidate bloom with wooden thumper |
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remove bloom and consolidate |
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charcoal |
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36 |
5 lbs |
180 lbs |
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return bloom to smelter |
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remove bloom and consolidate |
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charcoal |
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37 |
5 lbs |
185 lbs |
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return bloom to smelter |
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remove bloom and split |
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6:25 |
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smelt complete |
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Air
rates
Control Mark |
At mouth |
1" from mouth |
Fully Blocked |
m/s |
flow (L/s) |
m/s |
flow (L/s) |
m/s |
flow (L/s) |
A |
5.3 |
2.7 |
2.9 |
1.5 |
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A+ |
10.1 |
5.1 |
6.1 |
3.1 |
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B |
16.7 |
8.5 |
9.5 |
4.8 |
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B+ |
21.2 |
10.7 |
12.0 |
6.1 |
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C |
22 |
11.2 |
13.3 |
6.7 |
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C+ |
23.7 |
12.0 |
14.4 |
7.3 |
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D |
24 |
12.2 |
14.9 |
7.6 |
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D+ |
30.5 |
15.5 |
16.5 |
8.4 |
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|
The Anemometer has exactly a 1" diameter fan. The pipe has
an internal diameter of 1.375". The "At mouth" measurement is
done by placing the device against the pipe. This leaves 4
small holes where the air can escape with the majority going through
the device. The second sets of measurements are taken with
the device one inch from the mouth of the pipe. This provides
a feeling for the directness/pressure of the air. The final
column is measurements made with all air being forced through the
device (same as the first column but with the small holes blocked).
NOTES:
Charge times recorded at END of unit addition
* All charcoal charges are based on a 'standard pail' - weight of 5 lbs
All ore charges are based on a 'standard scoop' - weight of 3/4 lbs
Estimated from known marks
YIELD: 10 lbs (estimated) - looks like it may be good
workable iron (spark test on interior surface)
An excellent smelt.
This was as easy as it ever gets. We re-used the cob smelter from June,
so no construction work was required.
We started hauling out the piles of prepared gear at about 8 am or so.
Set the canvas and prepared the work area - about 9:30 Mounted the
ceramic tuyere, made new fittings to adapt the viewing T, patched a few
remaining cracks.
The air system preformed very well. We only had to 'roger' the tuyere
once, and might have been able to skip that one.
We did get a LOT of glassy gooey silica slag produced. Most of this was
extremely porous, so the volume was high. We should compare WEIGHT
against clay erosion some time. We had to tap this at least
three times, as the level rose to start flooding the tuyere. A big
crowd favorite!
We were concerned that we were not getting any of the iron rich 'gromp'
slag. When we sectioned the smelter the next day, it turned
out that there was an amount of this created, but it had run
through the lighter glass slag of the lower bowl to collect under the slag
bowl. We were able to pull this out as a single large piece.
Again, the slowest part of the preparation was the ore - with Ken and
Kevin doing the lion's share. We started with the richer taconite ore,
with 24 lbs prepared as the preheat was underway. One potential
error / problem from the post-smelt review. For the past couple of
smelts, wehave been roasting the pellets before crushing them. The material from
STELCO is not magnetic as it was delivered. This time we used the ore
pellets straight from source. This made the crushing more
difficult, and may have had an effect on our yield. In the end we added
a second lot of pre roasted Virginia rock ore (18 lbs).
There was also 1.1 Kg (2.4 lbs) of gromps (magnetic slag) left over
from the OABA smelt in May that was added near the end of the process. This
small amount, combined with the inability to access the newly created
iron rich slag, likely combined to produce the slightly porous
structure of the bloom.
Our process was halted partially by time, but also by the charcoal we
had prepared. In the end we had used 42 lbs of ore.
A solid 'slug' consisting of 1 1/2 lbs ore (two scoops) was then added
and allowed to settle to the bloom area. This judged by burn rate of the
charcoal. (5 more pail loads, 48 minutes of straight
charcoal. At this point the fire was allowed to burn down to about half
the smelter volume before extraction. The air flow was kept at the same
rate throughout the smelt (approx 12 L/s).
As with past smelts, the air was reduced and the top layer of burning
charcoal was scooped out down to roughly the top of the liquid slag /
tuyere level. (Since the sun had set at this point, the twilight made
for spectacular photos!) The thumper was used to loosen the bloom from
the slag bowl. The position was just as expected. This method has a
couple of advantages. It first removes the fragments of 'mother' that
cling to the bloom when it is extracted from the tap arch.
This makes the primary consoldation phase a bit easier. The second advantage
is that its easier to utilize the heated smelter as a giant forge
loading from the top.
The resulting bloom was positioned from the tip of the tuyere to about
the mid line of the smelter, but extending roughly from one side to the
other. This gave a rough lens shape roughly 10 x 5 x 5 cm.
It was roughly compacted using the wet stump method that Mike showed at
Early Iron (with good control). The hammer team was Ken, Dave and
Kevin. On the first compaction heat, the thickness was reduced by about
1/3. Three compaction heats were taken, reducing the size down to 6 x 5
x 2 1/2. There was virtually no fragmentation off the edges during the
process.We took a last heat to section for the classic 'pleiner
knotch'. Kevin on the hot set. The bloom cut relatively well. At about
1/2 way through, however, one of the lobes split off. (This same thing
happened at Early iron) The bloom most likely needed a bit more
compaction before cutting was attempted.
As mentioned, this smaller piece was later spark tested. The inside of
the cut surface was used. The sparks show large and red with
little feather, which suggests a good low carbon and workable iron was
produced.
The ceramic tuyere was exceptional. There was some, but actually very
little erosion. Over the entire course of the smelt, only
about one inch of the tubes lenght was lost. The crisp cyliner did errode
back to the classic conical shape encased with hard slag (as seen in
artifacts), We figure we can get at least two - maybe three uses from
each ceramic tube - at a cost of about $8 each.
The relining of the smelter proved sucessful as well. On Sunday the
smelter was sectioned along the tuyere line. This allowed us to
determine the relative erosion for the two uses of the structure. An
imporant note was that the higher erosion rate always experienced with
the metal pipe tuyeres had come close to completely burning through on
the last smelt. The 3" wall had been reduced to a mere 1/2 just above
the tuyere. On Saturdays smelt, less erosion was found, about 2" of
thickness remained (starting from roughly 3" thick). This is primarily
due to the durability of the ceramic tuyere. At the start of the smelt,
it projected about 2" from the interior wall. At
the end of the smelt it extended about 1 1/2 inches past wall (bearing
in mind that both the tuyere and wall had changed shape during the
smelt).
The position of the final slag bowl was about what was predicted for a
well managed smelt. The overall structure of the smelter, with the cob
cylinder resting on a circle of fire brick, created a problem. The
lower edge of the slag bowl was slightly below the upper rim of the
fire brick. This made first attempts to lower the slag bowl / decant
slag difficult. In the end the front brick had to be split and pulled
out in sections to allow access. If a large bloom had been desired,
this difficulty in lowering the slag bowl would have made it hard to
leave room for a larger bloom to form. This same restriction kept us
from gathering the iron rich slag that had formed and penetrated the
glassy slag at the last phases of the smelt. (Or frankly, even knowing
it was there.)
Taken altogther, and extremely successful smelt!
One new experimental process proven - that of relining the smelter.
There was some discussion of attempting a third use of this smelter.
There was extensive cracking of the structure, with pieces missing from
the top edge. More importantly, the area around the tap arch was in
pretty poor shape. There was a large block of solidified slag that
would have had to have been chipped out, with probable damage to the
base area. It was decided that it would be better to build a new
smelter for next years series. Clearly though with additional
forethought we can set a tap arch we won't have to damage as much to
get the slag out.
One new piece of equipment tested and proven - the ceramic tube tuyere.
The durability of this was excellent, and is combined with the low unit
cost and ease of replacing. (almost as good as the heavy forged copper
tuyere - and at 1/10 the cost). A new mounting pipe will be made up to
match the ceramic to the existing T port system.
|
Reports of all of our iron smelting efforts along with more articles and information are available on the "Iron Smelting in the Viking Age" CD from the Wareham Forge. Copies of the CD can be purchased here. |